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RX-7 Rebuild Notes | |||||||
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Start Date: March 2, 2003 |
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After 75,000 miles my motor has finally given up and is having intermittent overheating problems. Apparently the water seals had started to detoriate and now there are hydrocarbons in the coolant and slight signs of coolant on my spark plug tips. These are sure signs of bad water seals. I am guessing that my problems started when my radiator burst about a year and a half ago in Sacramento. The engine was probably weakened a great deal in that mess but was still going ok. I think as time went on I had more and more cold startup white smoke from the coolant in my engine too. After doing a few months of research of what to do I have decided to attempt to replace my old engine (and original) with a new Mazda Remanufactured engine from Malloy Mazda. Although I have heard mixed reviews on these engines (of course you should take everything you hear with a grain of salt on the internet...especially message boards) I do believe they offer the best bang for the buck out of all options out there. The entire engine removal and installation will be taking place in my single car garage here in San Francisco. This is a huge project for me since I'm just a shadetree mechanic and don't have access to any airtools and have never even dropped my tranny before. I hope for the project to be completed in about 3 weeks if everything goes smoothly. With my track record of breaking little parts etc. though it will probably take twice as long. Let's get started. | |||||||
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Sunday March 2nd, 2003 After taking out my water pump months ago to make sure it was not the culprit of my overheating problems I needed to put everything back together in order to drive my car out and turn it around. Otherwise, I wouldn't be able to get the engine hoist or new engine into the single car garage. I couldn't just push the car out of garage and turn it around because there is quite steep slope leading up into the garage and fire hydrant close enough to the door to discourage me from taking that route. So basically the first day I spent and hour or two putting everything together again to turn the car around. These are all the steps I took in the actual engine removal.
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Thursday March 6th, 2003 I spent about an hour tonight taking out some easy stuff. These items don't really require anymore detail in their removal procedure.
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Friday March 7th, 2003 The first real working day allowed me to finally get some real work done. The goal was to get the car almost up to the point of pulling out the the engine and tranny as a whole unit. There are only a few thing left to be completed in order to pull the engine and tranny out. Something weird to not...my clutch release cylinder had the lower bolt sticking out about 1/2 inch. This is kind of freaky because my friend Reza said the same thing happened to his except for both bolts were loose. Something to look out for in the future.
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Saturday March 8th, 2003 Success! The engine is out of the car and sitting on an old motorcycle tire in the garage. With the help of Reza and Calvin (also true RX-7 fanatics) we got the engine and tranny out by 8pm. I worked on the engine by myself for about 2 hours this morning retapping one of the upper intake manifold bolt holes that holds the engine hook. I spent a whole bunch of time fighting with the nuts between the main catalytic converter and catback too. Those suckers were on there tight and rusted but a couple quenches of liquid wrench, some tapping, some swearing, and a 3 foot breaker bar it came off. Of course I had to put my downpipe back on to give myself more torque on the nuts which I should have just done in the first place! Reminder to self: Loosen those nuts before removing downpipe next time to avoid wasting hours.... Hoisting out the engine was actually the most fun and quickest part of the whole process. Pulling the ECU harness through the firewall was a trip too. We had to loosen the wiper arm motor to get better access to the harness and big grommet that holds it in the firewall. Tracking all the places the driver's side ignition harness connects to was fun as well. Everything is detailed down below.
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Monday March 10th, 2003 I took off the turbos and exhaust manifold on this day for inspection. There is huge crack in between the primary turbo exhaust port and the secondary pre-spool but the turbos still boost fine. I think I will use them till they die completely.
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Friday March 14th, 2003 The engine arrived today from Malloy after being shipped all the way from Virginia over the course of 4 days. I highly recommend ordering an engine from them. It is easy and they have great service. I also installed a 2nd oil cooler on the passenger side. This was a broken oil cooler off a 2000 RZ clip but I had it fixed and it'll work great now...
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Saturday March 15th, 2003 I started swapping some little parts and disassembling the old motor today taking off the accessories. I also took the time to tap the new thermostat housing to fit the stock water temperature sensor. I have my Greddy sensor mounted in the stock location while the stock on resides in the thermostat housing. The tap required to do this is a M10 1.00 pitch. That is a very very fine pitch for a hole that big and is a rather obscure size. The drill size required it a 24/64" or 9.1mm which was also hard to find so I just used a 11/32" which was 1/64" off but worked well.
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Monday March 17th, 2003 Wow this project really is taking a lot out of me. I just finally completed stripping the old block of just about everything and started swapping the old stuff to the new block. The significant things I completed today was switching out the weak solenoid rack bolts with new grade 5 hex bolts of the same length. The old ones come off with a phillips head screwdriver and are easy to strip. This is probably obvious to anybody who has done the vaccuum hose job. Replacing the 11 bolts with the new M5 0.8 pitch (standard pitch) will make taking them off with a hex a breeze. The 3 bolts near the firewall are almost impossible to remove normally. I also picked up a used Jspec downpipe from my friend Calvin. It is just like a US downpipe except there is no catalytic converter so it is just a straight pipe. It will definitely fit better than my messed up M2 downpipe. I'll be getting rid of my EGT sensor in the process and replacing it with a new Greddy Oil Pressure sensor that I received from rx7.com today.
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Saturday March 22nd, 2003 Today the new Racing Beat Flywheel went on. I weighed both the stock one and the Racing Beat Flywheel/Counterweight to get a better idea of what the weight savings would be. I weighed the components on my Tanita digital scale that has resolution down to 0.2 lbs. The weights turned out to be the following: Stock: 20.4 lbs. Racing Beat: 8.0 lbs. + 4.0 counterweight = 12.0 lbs. The weight lost with the lightweight flywheel turns out to be 8.4 lbs. or 41.4%. However, looking at the picture you can also tell that much of the stock flywheel's weight is on the outside of the wheel versus the Racing Beat which has basically an even spread of mass over its radius. This mass on the stock wheel means that the rotational inertia loss is probably greater than 50%. Most likely is it around 60%-65% less. This is just by me eying the wheel and guesstimating though. I didn't do any math other than what is above. Anytime you put on a tranny you should have the clutch alignment tool. Well that's at least my take on it since it only costs a couple bucks. It probably would have saved us about an hour versus trying to figure out whether we were going to align it by eye or tighten the pressure plate after the tranny was one. It finally went on though. I think that is all we did this day. I'm trying to remember this from about 2 weeks ago as I write this.
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Sunday March 23rd, 2003 We finally dropped the engine/tranny back into the car today. Let me say this....dropping the engine in is way harder than taking it out. It took us about 5x longer.....we ran into a couple problems some people probably would not run into. First, the surface of my garage is not perfectly level. The whole thing is slightly on a downgrade with the garage door being the bottom. There is also a small drainage grill where the engine hoist needs to reside when putting the engine in the car. Second, the hoist we were using has an arm that is not quite long enough at the setting we were using it at (500 lbs). This meant the front of the hoist was hitting the bumper which was made worse by the incline of the garage! No damage though. By the time we had dropped the engine in we were dead tired because we also went to the SCCA autocross that morning. We basically were toast after that and just let the car rest for the remainder of the night too. Just to add, we spent some time rerouting the engine wiring harness because not all the connectors were reaching their destinations on the UIM. What a nightmare!
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Sunday March 30th, 2003 Well, I felt completely sick the past week while struggling to get the rest of the parts hooked up to the car. I seriously think I inhaled too many toxic chemicals. Reza came by today to help me get everything else hooked up and we started the car. It was nice to finally see where we were at. It started up on the first try but died immediately because there wasn't enough gas. Starting it the second time yielded a successfuly idle and every looked normal until....I noticed the low coolant buzzer going off and there as a small stream of coolant coming from the passenger side behind the wheel. So much for our midnight joyride! We jacked up the car and I figured out the coolant was leaking from the heater core copper pipe that I had...uhumm....bent out of shape when changing out the silicone heater hose.....my mistake. So, we gave up for the night and let the whole thing rest again.
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Thursday April 3rd, 2003 So close yet so far away. After an entire month of working on the project I was very frustated at this point. I had fixed the coolant leak with a new clamp but now had a new mysterious problem that was holding me back. Oh yeah, I had installed the new oil pressure gauge and redid some wiring in the meantime. The problem was a loud, high-pitched, metal on metal fluttering sound when revving up the engine above 1800 rpm. The car drove great other than this sound. At first I thought it was the belts squeaking but adjusting them did nothing. I then replaced the airpump. Three times! All of these pumps still gave me the same sound. I finally localized the sound down to somewhere underneath the upper intake manifold. Any key symptom to the problem was that when the airpump connector was disconnected the sound went away. Therefore, the sound had to come from something to do with the secondary air injection system designed for emmisions. I was about to swap to a midpipe and ditch all thi stuff when I decided to take out the ACV and test it. What a PIA it is to remove all this junk just when you are about to seriously drive your car for the first time in 5 months! Well, I took out the ACV and had to wait until the next day to buy a vaccuum tester to test it....All this stuff had happened earlier in the week. Thursday I went down to Reza's to check out the ACV he had. We tested both of them and they both performed flawlessly. Wonderful, what could it be then? After dinner, Tapioca drinks, and almond cookies, we finally figured out it was the 1" round check valve that was making the noise. The tell-tale signs of this were an elliptical shaped smashed carbon on the back of the check valve. There was also a new black mark on the LIM from the check valve being squeezed by it and the acv in the incorrect position. Thanks to Will at C2 Automotive and Reza for helping me troubleshoot this one....reinstallation commenced the next morning...
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Friday April 4th, 2003 Well, after reinstalling the acv,uim,ic, etc. i started up the car and to my surprise there was no more fluttering sound! Problem solved. Looked underneath the car and zero leaks! Hooray! I readjusted the idle and it was time for the test drive. I took it about 125 miles today. Most of the miles I did on PCH between SF and Santa Cruz. It was a great day out weather wise and was just enhanced by my excitement to finally drive my RX-7 today. What a day. I did not encounter any problems and everything was running smoothly. Looking back I'm happy I took on this huge project. Not only did it save me a little bit of cash but it was a huge learning process from a technical RX-7 point of view and a project management experience. Thanks to Reza, Calvin, Adrian, and Will for all their help. One big huge thanks to my girlfriend, Anna, who was patient with me the whole month even though I spent most of it in the garage! Thank god it is done!!! I took a pic of a nice secluded beach to say farewell with. If you got this far reading I hoped you enjoyed my write up. E-mail me at alexwan@alexwan.com if you have any questions. Till next time................ ~Alex
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| RX-7 Rebuild Notes | alexwan.com | ||||||